Increase Performance Increase Performance

Burner Modification Projects - We offer a full line of Fired Process Solutions!

Ammonia Plant Before and After
Down Fired Kellog Reformer Furnace
Down Fired Kellog Reformer Furance Down Fired Kellog Reformer Furance
  • Poor distribution of radiant heat
  • Excessive heat on burner tiles
  • Burner tile failure falling damaging tunnel refractory
  • High process tube temperature near burners
  • At firing capacity on burners
  • High NOx.
  • Excellent even radiant heat
  • No overheating tiles
  • Damage eliminated
  • Process tube temperature normal
  • 22% additional firing capacity
  • 40% NOx reduction
  • 1-2% increase in efficiency
Radiant Wall Selas Furnace - California low NOx package available
Radiant Wall Selas Furnace Radiant Wall Selas Furnace
  • At maximum firing capacity
  • Poor flame shape projecting towards process tubes
  • High process tube metal temperatures
  • Excess CO, no excess oxygen
  • 30% additional firing capacity
  • Excellent flame shape for radiant heat transfe
  • Normal process tube temperatures
  • CO eliminated and 24% excess oxygen achieved
  • Major efficiency improved with payback in less than 6 months
  • California low NOx package available
Chemical Plant Before and After
Firebox Reformer Furnance
Firebox Reformer Furnance Firebox Reformer Furnance
  • Process tube metal temperature
  • Restricting production
  • Less tube life
  • At maximum burner firing capacity
  • Flames too short for optimum transfer
  • Very high noise
  • High NOx
  • Process tube metal temperatures reduced substantially below limit
  • Production increase
  • Burner firing capacity increased by 15%
  • Even dispersed radiant flame for maximum heat transfer
  • Reduced NOx
  • Substantial noise reduction
Petroleum Refinery Before and After
Major efficiency improved with payback in less than 6 months
Rectangle Process Heater
Rectangle Process Heater Rectangle Process Heater
  • Poor flame shapes
  • Radiant heat transfer erratic
  • Constant burner gas plugging
  • Full time maintenance required
  • Wasted fuel gas
  • High convection tube temp
  • Excellent uniform flame shape
  • Optimum radiant heat transfer
  • Zero maintenance-saving $70K/yr
  • All process tube metals normal

Contact us today for additional information and to obtain a direct referral from our satisfied clients.